Challenge

A customer had a screen application
utilizing worm and wheel gearboxes mounted
vertically at the bottom of the screens. The
component style seal in the gearbox was leaking
prematurely, causing bearings in the gearbox to
fail, ultimately damaging the gearing.
Solution

Applied created a bearing cartridge
solution, built in-house, that utilized a
positive drive belt system. The new
configuration was lighter and incorporated a new
cartridge mechanical seal and a bearing isolator
to protect the bearings.
Savings

The customer has realized significant
savings from improved equipment reliability in
addition to hard cost DVA savings from Energy
Savings and Reduced Maintenance Costs totaling
more than $25,000 annually.
Challenge

A customer experienced an emergency
breakdown to an application using an expensive
mechanical seal. The replacement seal had a 3
day lead time that would leave the customer’s
operation shut down, resulting in substantial
lost production.
Solution

An Applied representative visited the
maintenance point to inspect the application and
discovered that the mechanical seal in question
was not accomplishing the task for which it was
intended to do. The Applied representative
suggested that a traditional oil seal would
perform as well as the mechanical seal, and
could be provided in a matter of hours at a
fraction of the cost.
Savings

The customer realized $8,977 in
increased uptime and price savings
Challenge

A customer was experiencing
damaged product caused by a steep elevation
change at a belt conveyor transfer point.
Solution

The Applied Technical Services
Group worked with the Applied Sales Rep and
customer personnel to fabricate a spiral shoot
to install at the transfer point, allowing
product to make a controlled descent, lessening
the impact at the bottom of the transfer point.
Savings

The customer estimated savings of more
than $50,000 annually, resulting from less
product being damaged and needing to be
re-circulated.
Challenge

A food products company was
having
problems with product tipping and jamming the
conveyor.
Solution

Applied switched the conveyor
chain, which
stopped the product from tipping.
Savings

This change provides an extra 30 minutes
a day
of production and $72,000 in annual downtime
savings.